Creality CR10S: Difference between revisions

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[[File:Placeholder.jpg|300px]]<br/>
[[File:Creality_CR10.jpg|300px]]<br/>
'''Location:''' Electronics Room <br/>
'''Location:''' Electronics Room <br/>
'''Ownership:''' MAG Laboratory <br/>
'''Ownership:''' MAG Laboratory <br/>
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== Description ==
The Creality CR-10S V1 is a cartesian 3d printer with a relatively large build volume.  It is built primarily using 4040 and 4080 extruded aluminum with the beams running on the X axis being constructed of 4040 aluminum and all other beams being constructed of 4080 aluminum.  The axes on the CR-10S are constructed using shielded bearings and acetal running wheels which provide maintenance free operation.  The axes are constructed in a Prusa format with the Y axis moving the build plate, the X axis moving the extruder, and the Z axis moving the X axis carriage.
== Software ==
Cura has been used to slice models for loading onto this printer.  It takes Marlin-flavor G-code.
=== Start Code ===
<pre>
M201 X500.00 Y500.00 Z100.00 E5000.00 ;Setup machine max acceleration
M203 X500.00 Y500.00 Z10.00 E50.00 ;Setup machine max feedrate
M204 P500.00 R1000.00 T500.00 ;Setup Print/Retract/Travel acceleration
M205 X8.00 Y8.00 Z0.40 E5.00 ;Setup Jerk
M220 S100 ;Reset Feedrate
M221 S100 ;Reset Flowrate
G28 ;Home
M420 S ;Activate bed leveling
G92 E0 ;Reset Extruder
G1 Z2.0 F3000 ;Move Z Axis up
G1 X10.1 Y20 Z0.28 F5000.0 ;Move to start position
G1 X10.1 Y200.0 Z0.28 F1500.0 E15 ;Draw the first line
G1 X10.4 Y200.0 Z0.28 F5000.0 ;Move to side a little
G1 X10.4 Y20 Z0.28 F1500.0 E30 ;Draw the second line
G92 E0 ;Reset Extruder
G1 Z2.0 F3000 ;Move Z Axis up
</pre>
== Firmware ==
The 3d printer was configured using the configuration file example found in <code>Creality/CR-10S/CrealityV1</code> and Marlin version <code>2.0.9.5</code>.  Future changes may include adding more bed leveling points and an upgrade to the latest version of Marlin.  Additionally, the leveling grid may start from the previously recorded leveling point instead of starting at a 0.2mm offset.


== History ==
== History ==
Line 38: Line 68:
The build surface was blue tape when the printer was first donated.  The build surface was the Creality "Carborundum" tempered glass bed.  As of 2022-08-22, the bed is binder-clipped, PEI coated steel.
The build surface was blue tape when the printer was first donated.  The build surface was the Creality "Carborundum" tempered glass bed.  As of 2022-08-22, the bed is binder-clipped, PEI coated steel.


== Operator's Log ==
=== Controller ===
==== 2022-08-26 Yangbot ====
The mini USB B connector on the controller board was previously destroyed.  The printer is now connected to octoprint using a hardwired USB A cable.  Thanks Yangbot.
 
== Operators' Log ==
==== 2022-08-26 Yangbot, entered by [[User:Blu | Brandon]] ====
Bed adhesion issues noted when printing bike handlebar spacers.
Bed adhesion issues noted when printing bike handlebar spacers.


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[[Category:3D_Printers]]
==== 2022-09-02 [[User:Blu | Brandon]] ====
Nozzle was severely clogged with burnt plastic.  Nozzle replaced.
 
The clogged nozzle could have caused the issues on 2022-08-26, but a bed leveling was also performed.  Additionally, extrusion on the first layer is increased to 120%. 
 
==== 2022-09-03 [[User:Blu | Brandon]] ====
Bed leveling completed and [https://www.printables.com/model/241627-260-to-318-mm-handlebar-shim bike handlebar adapter from Thingiverse] successfully printed.
 
The bed is still severely unlevel in the middle and center-right corner.
 
In order to adhere to the rough PEI surface, the printer was leveled 0.1mm lower than the measured height.  This is done so that the first layer of extruded plastic will flow around the rough PEI coated texture on the bed and create a stable mechanical bond.
 
==== 2022-11-30 Betsy, entered by [[User:Blu | Brandon]] ====
USB port broken during printer shuffling and repaired/replaced by the yangbot.
 
Although it was once an issue, it is no longer an issue.  Do not place stress onto the USB connector and always check the print area for things that may come into contact with the printer while it is in motion.
 
==== 2022-12-06 [[User:Blu | Brandon]] ====
The last print performed yesterday at 2022-12-05 23:50 did not succeed.  The filament was not loaded during the print, and a first-layer inspection was not completed.
 
Nozzle is further from the printer platform than normal.  This may be the result of a previous maintenance action on the 3d printer or from a previous operator failing to save the printer bed leveling data into EEPROM.
 
The issues were resolved by turning bed leveling on before starting the print.  <code>m420 s1</code> applies bed leveling and should be run after the printer homes axes.
 
==== 2022-12-14 [[User:Blu | Brandon]] ====
Previous operator logs did not note other dips in the 3d printer surface between the center and rearmost leveling points.  It is theorized that a more granular UBL grid would be able to compensate for these points in the future.
 
The fan was replaced with the Y.S. Tech YW04010012BSS previously selected for the Zortrax.  Although the printer probably works, it is was placed into delta stale status since a minor qualification print with the new fan is required.
 
The printer successfully printed the camera angler upgrade for itself on the same day, and the printer was removed from stale status.
 
==== 2023-01-05 [[User:Blu | Brandon]] ====
Print completed without note.
 
==== 2023-01-10 [[User:Blu | Brandon]] ====
"Travel :: Extrusion Combing" turned off in Cura; it should have been on the entire time.  This setting was changed to "Not on outer surface."
 
==== 2023-03-09 [[User:Blu | BLu ]] ====
YACS printing was successfully completed on this printer.  It is recommended that the fan speed be adjusted since the printer exhibited print curl during YACS printing.
 
The printer also experienced a collision with the cables connecting to the X axis carriage and this caused the carriage to become un-level.  The carriage and bed were leveled and the printer was tested with YACS again.
 
==== 2023-04-01 [[User:Blu | Brandon ]] ====
Printing with PETG led to strange inconsistencies that may be related to hydrated filament.  These largely interfered with the attempted transparent printing.
 
It is noted that a comprehensive list of changed settings has not been posted to the wiki.  This section aims to fix that deficiency.  The following settings are applied to the printer:
{| class="wikitable"
! | Section || Setting || Value
|-
|rowspan=2| Quality || Initial Layer Height || 0.3 mm
|-
| Initial Layer Line Width || 150 %
|-
| Material || Initial Layer Flow || 105 %
|-
|rowspan=2| Speed || Initial Layer Speed || 12 mm/s
|-
| Enable Acceleration Control || ✅
|-
|rowspan=6| Travel || Retraction Distance || 4.0 mm
|-
| Retraction Speed || 60 mm/s
|-
| Retraction Minimum Travel || 1.0 mm
|-
| Combing Mode || Not on Outer Surface
|-
| Z hop when Retracted || ✅
|-
| Z hop Height || 0.4 mm
|-
|rowspan=2| Build Plate Adhesion || Build Plate Adhesion Type || Brim
|-
| Brim Width || 4.0 mm
|-
| Walls || Z seam Alignment || Shortest
|}
 
== Other 3D Printers ==
This is a part of our ongoing effort to document our 3D printers.
{{Template:3D_DigitalFabrication}}
[[Category:3D Printing]]

Latest revision as of 19:22, 17 March 2024

Creality-CR10S

Creality CR10.jpg
Location: Electronics Room
Ownership: MAG Laboratory
Status: Fully Working
Usage Restrictions: N/A

3D Printer

Brand: Creality
Model: CR10S
Type: Cartesian
Quality: Hobby
Build Volume:

  • Length: 300mm
  • Width: 300mm
  • Height: 400mm

Materials: ABS, PLA, PETG
Nozzle Size 0.4mm

Description

The Creality CR-10S V1 is a cartesian 3d printer with a relatively large build volume. It is built primarily using 4040 and 4080 extruded aluminum with the beams running on the X axis being constructed of 4040 aluminum and all other beams being constructed of 4080 aluminum. The axes on the CR-10S are constructed using shielded bearings and acetal running wheels which provide maintenance free operation. The axes are constructed in a Prusa format with the Y axis moving the build plate, the X axis moving the extruder, and the Z axis moving the X axis carriage.

Software

Cura has been used to slice models for loading onto this printer. It takes Marlin-flavor G-code.

Start Code

M201 X500.00 Y500.00 Z100.00 E5000.00 ;Setup machine max acceleration
M203 X500.00 Y500.00 Z10.00 E50.00 ;Setup machine max feedrate
M204 P500.00 R1000.00 T500.00 ;Setup Print/Retract/Travel acceleration
M205 X8.00 Y8.00 Z0.40 E5.00 ;Setup Jerk
M220 S100 ;Reset Feedrate
M221 S100 ;Reset Flowrate

G28 ;Home
M420 S ;Activate bed leveling

G92 E0 ;Reset Extruder
G1 Z2.0 F3000 ;Move Z Axis up
G1 X10.1 Y20 Z0.28 F5000.0 ;Move to start position
G1 X10.1 Y200.0 Z0.28 F1500.0 E15 ;Draw the first line
G1 X10.4 Y200.0 Z0.28 F5000.0 ;Move to side a little
G1 X10.4 Y20 Z0.28 F1500.0 E30 ;Draw the second line
G92 E0 ;Reset Extruder
G1 Z2.0 F3000 ;Move Z Axis up

Firmware

The 3d printer was configured using the configuration file example found in Creality/CR-10S/CrealityV1 and Marlin version 2.0.9.5. Future changes may include adding more bed leveling points and an upgrade to the latest version of Marlin. Additionally, the leveling grid may start from the previously recorded leveling point instead of starting at a 0.2mm offset.

History

The Creality-CR10S was donated by Kyle. Thanks.

The glass build bed was donated by Michael.

Hotend

The hotend was previously clogged with a giant blob of PLA. Please watch your prints through the first layer at least. Not all prints will succeed, but you are more likely to succeed after the first layer is printed.

The thermistor on the hotend was replaced on 2022-07-20. Problems were noted in June.

Bed

The build surface was blue tape when the printer was first donated. The build surface was the Creality "Carborundum" tempered glass bed. As of 2022-08-22, the bed is binder-clipped, PEI coated steel.

Controller

The mini USB B connector on the controller board was previously destroyed. The printer is now connected to octoprint using a hardwired USB A cable. Thanks Yangbot.

Operators' Log

2022-08-26 Yangbot, entered by Brandon

Bed adhesion issues noted when printing bike handlebar spacers.

2022-08-28 Brandon

Bed adhesion issues confirmed.

Bed leveling was completed successfully, but there is a significant dip in the center and center, right side of the 3d printer bed. Bed leveling shows concerning data:

0.2mm leveling data
0.225 0.225 0.275
0.225 -0.050 0.000
0.275 0.250 0.300

2022-09-02 Brandon

Nozzle was severely clogged with burnt plastic. Nozzle replaced.

The clogged nozzle could have caused the issues on 2022-08-26, but a bed leveling was also performed. Additionally, extrusion on the first layer is increased to 120%.

2022-09-03 Brandon

Bed leveling completed and bike handlebar adapter from Thingiverse successfully printed.

The bed is still severely unlevel in the middle and center-right corner.

In order to adhere to the rough PEI surface, the printer was leveled 0.1mm lower than the measured height. This is done so that the first layer of extruded plastic will flow around the rough PEI coated texture on the bed and create a stable mechanical bond.

2022-11-30 Betsy, entered by Brandon

USB port broken during printer shuffling and repaired/replaced by the yangbot.

Although it was once an issue, it is no longer an issue. Do not place stress onto the USB connector and always check the print area for things that may come into contact with the printer while it is in motion.

2022-12-06 Brandon

The last print performed yesterday at 2022-12-05 23:50 did not succeed. The filament was not loaded during the print, and a first-layer inspection was not completed.

Nozzle is further from the printer platform than normal. This may be the result of a previous maintenance action on the 3d printer or from a previous operator failing to save the printer bed leveling data into EEPROM.

The issues were resolved by turning bed leveling on before starting the print. m420 s1 applies bed leveling and should be run after the printer homes axes.

2022-12-14 Brandon

Previous operator logs did not note other dips in the 3d printer surface between the center and rearmost leveling points. It is theorized that a more granular UBL grid would be able to compensate for these points in the future.

The fan was replaced with the Y.S. Tech YW04010012BSS previously selected for the Zortrax. Although the printer probably works, it is was placed into delta stale status since a minor qualification print with the new fan is required.

The printer successfully printed the camera angler upgrade for itself on the same day, and the printer was removed from stale status.

2023-01-05 Brandon

Print completed without note.

2023-01-10 Brandon

"Travel :: Extrusion Combing" turned off in Cura; it should have been on the entire time. This setting was changed to "Not on outer surface."

2023-03-09 BLu

YACS printing was successfully completed on this printer. It is recommended that the fan speed be adjusted since the printer exhibited print curl during YACS printing.

The printer also experienced a collision with the cables connecting to the X axis carriage and this caused the carriage to become un-level. The carriage and bed were leveled and the printer was tested with YACS again.

2023-04-01 Brandon

Printing with PETG led to strange inconsistencies that may be related to hydrated filament. These largely interfered with the attempted transparent printing.

It is noted that a comprehensive list of changed settings has not been posted to the wiki. This section aims to fix that deficiency. The following settings are applied to the printer:

Section Setting Value
Quality Initial Layer Height 0.3 mm
Initial Layer Line Width 150 %
Material Initial Layer Flow 105 %
Speed Initial Layer Speed 12 mm/s
Enable Acceleration Control
Travel Retraction Distance 4.0 mm
Retraction Speed 60 mm/s
Retraction Minimum Travel 1.0 mm
Combing Mode Not on Outer Surface
Z hop when Retracted
Z hop Height 0.4 mm
Build Plate Adhesion Build Plate Adhesion Type Brim
Brim Width 4.0 mm
Walls Z seam Alignment Shortest

Other 3D Printers

This is a part of our ongoing effort to document our 3D printers.